This last weekend I loaded up my kart along with the karts of my brother and father. In the midst of all of that, I twisted my ankle pretty good. I was not going to let that get in the way of testing out my freshly rebuilt Honda GX200 Modified. Yes that is correct, no longer do I have a clone modified. After tearing the motor down to fix the issue with the head we decided to take everything out. It had been a few trips to the track since I had completely taken the motor apart and I wanted to see how everything was wearing. My father, who has had a bit more spare time then I, spend the time taking it apart and reporting his findings to me.
The wear on the remaining clone parts that were in the motor was minimal. I have been really impressed with how some of the clone components hold up. The block looked great, with minimal cylinder wear considering the many times I have taken that motor over 9,000 RPM. At this point the only clone components that were left was the block, bearings, crank and side cover but they all still looked in great shape.
Being that I had a new stock Honda GX200 motor sitting on my bench I decided to put my modified parts on the Honda and use my clone as a semi-stock backup motor. The original plan for the Honda was to build an open motor but I have since decided against spending more money on motors and decided to move the parts over to the Honda. The stronger block and crankshaft will help me sleep better at night. My old clone block is going to receive a flat top Honda piston, Honda rod, Dyno CS Cam, 1.3:1 stamped rockers and a blueprinted carb. This motor will be placed on my Margay which I hope to make my backup kart soon. It will also serve as a good kart to have friends drive when I go to the track.
This weekend we decided to go to Prairie City since the Stockton track has been closed down. Prairie City is a fun and brutal track with a lot of tight corners. I was excited to be there as I had not driven that track in over 15 years. Saturday was a practice day before a club race the next day so there was a few karts out there. I was surprised to find there was a few drivers sporting modified YF200 motors. Anything other then stock clones was a sight for sore eyes. There was one other modified clone out there but I did not get to see it run on the track.
The YF200′s were pretty quick. I had never seen one in person so I was very interested to see one run. I know about them but I had never seen one on the track. I went out for my first trip around the track to break in my motor and my clutch. My motor had not yet been ran, except for 10 minutes at idle on the stand, and my clutch was completely new. I was very excited about my SMC Vortex Clutch. I felt that this clutch was going to change my life forever.
After the break-in session I went back out for a few more laps at a medium pace before putting a few hard laps on it toward the end. I felt good about my motor. It ran strong. I was peaking at about 8,900 RPM and needed a geer change. The track is so tight that I was losing a lot of momentum in the corners and could not come out of it like I should with the chosen gearing of a 4.75 ratio. I added 3 teeth to the rear sprocket and gave it another go.
I had the power I was missing in the corners, for the first two laps that is. After that, my motor seemed to bog way down in the corners, so I started adjusting my carb. When that didn’t help, I tried driving harder through the corners to keep my RPM up. That didn’t seem to help much either. After about 5-6 laps of trying, I gave up and came in. When I was almost off the track I noticed that my clutch was not disengaging. My new Vortex clutch was stuck, so I rolled to a stop.
After getting out I looked down and saw a disc hanging out of the clutch. The clutch drum had locked up on to it’s shaft causing it to be locked up. The outer disc that was hanging out was a bit chewed up from grinding on the outside of the drum and there was some wear on the outer plate that the disc normally sat inside of. The clutch looked to be in pretty bad shape. It probably got quite hot. I was really frustrated. The paperwork that came with this clutch promised it to be for large engines and for the most part worry free. At the price tag it carries I was not happy. I ordered the clutch from APS, whom I called today. I hope to get at the very least a replacement clutch. My motor seems to just destroy clutches even though the Vortex clutch is suppose to handle motors much more powerful than mine. One of the YF200′s had the same clutch and he said he does not have any issues with his. My last trip out on the track when the clutch problem occurred was with the YF200. He was able to stay on my tail through the corners when I couldn’t keep my RPM up due to the locked up clutch. Regardless, I was still pretty impressed with the power those YF200′s put out. I am not sure how much was done to his motor in comparison to my motor. On the straight away I was just as fast as a TAG however out of the corners they pulled on me quite a bit. Even before the clutch issues
came about I needed more RPM through the corners. We had the Vortex clutch set to the second to last setting.
So where does this leave me? I am not really sure. I am really considering giving up this modified stuff for a while. It is just to much work for someone who does not have the time to keep up with it. I have been a bit to busy this year which has kept me from spending much time on the kart. What I really need is a kart that is fast and worry free, however that doesn’t make much sense now does it.
I have some pictures of the damaged Vortex clutch I will post later along with the results of my conversation with APS. As for my Modified Honda GX200… I am not sure if I am going to keep it or not. Time will tell…